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@h0bbl3s h0bbl3s commented May 22, 2025

Correct the PID_YAW settings to fix the yaw washout issue and improve flight, as well as disabled dynamic idle.

h0bbl3s added 7 commits May 21, 2025 21:12
Correct the PID_YAW settings to fix the yaw washout issue
Lowered I-term on yaw
Added correction for dynamic idle
Further reduced dynamic idle to increase stablity
Final Tune
- found a good middle ground on dynamic idle
- increase feedforward on yaw for responsiveness
Discovered the dynamic idle was never intended to be on, introduced an override. This should disable dynamic idle and return the motors to static 8% idle.
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